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@AtomPod, thanks for the report. I ran a quick mission using master and there seems to be some issues with the params. The plane achieves > 13m/s in CIRCLE but was not completing circuits on an AUTO mission - so something may have changed in recent versions of the firmware that requires a retune?
If you could post the log*.bin from your test that would be helpful.
I used the following command for simulation, but the speed has been between 1~2m/s after takeoff
but I tried using skywalker_x8_quad, it worked fine
gazebo: gz sim -v4 -r alti_transition_runway.sdf
ardupilot(version 4.4): sim_vehicle.py -v ArduPlane --model JSON --add-param-file=$HOME/ardupilot_gazebo/SITL_Models/Gazebo/config/alti_transition_quad.param -f quadplane --console --map
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